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Sunday, 17 May 2015

First flight for the new quad

It took a while to sort this one out. It was quite stable on the cc3d flight controller, but when using the flip32 it would not fly! After some work I found that one of the four QBrain speed controllers had been set to Ni- battery type and not Lipo.

Needed to repair the landing skids after the first bad flight on the flip32!

Posted by Andy at 04:59
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Labels: Multirotor
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